Ingeniería en Sistemas, Electrónica e Industrial
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Item Redistribución de planta en la empresa Jambi Kiwa(Universidad Técnica de Ambato. Facultad de Ingeniería en Sistemas, Electrónica e Industrial. Carrera de Ingeniería Industrial, 2024-08) González Flores, Yolanda Patricia; Rosero Mantilla, César AníbalThis study deals with the plant redistribution in Jambi Kiwa, a company dedicated to the production and commercialization of aromatic and medicinal herbal teas. Key aspects such as process design, micro-location of the facility and functional configuration were considered. In addition, the operations for obtaining the herbal teas, the distance traveled by the collaborators and the flow of activities in each production area were analyzed. The optimal redistribution combined batch and product distribution. The Systematic Layout Planning (SLP) method was used to establish relationships and priorities between areas, minimizing distances traveled. In addition, the Guerchet Method was used to determine the areas required at each work center. Corelap 01 software helped to identify the ideal layout of the areas, prioritizing the areas of closest proximity. Using these criteria, a layout was designed to maximize operational efficiency and improve overall productivity, and four proposals were developed. To select the best option, a load-distance analysis was performed, evaluating the efficiency of each layout in terms of proximity and material flow. FlexSim software was also used to simulate and validate the proposals, ensuring workflow optimization. Proposal D turned out to be the most efficient, achieving a 10.60% reduction in the total distance traveled, equivalent to 351.25 meters, which significantly improves the work flow. This proposal, with a cost of $ 3000.16 for the operational and productive optimization of the plant.Item Redistribución de instalaciones en la planta de producción de la empresa Ambasodas(Universidad Técnica de Ambato. Facultad de Ingeniería en Sistemas, Electrónica e Industrial. Carrera de Ingeniería Industrial en Procesos de Automatización, 2022-09) Cárdenas Jácome, Andrés Sebastián; Ortiz Sailema, Christian IsmaelItem Estudio de tiempos y movimientos para la mejora de la productividad en la empresa Compubordado(Universidad Técnica de Ambato. Facultad de Ingeniería en Sistemas, Electrónica e Industrial. Carrera de Ingeniería Industrial en Procesos de Automatización, 2022-09) Gutierrez Veliz, Luis Roberto; Gavidia García, José LuisThe main objective of this research work is to improve productivity in the COMPUBODADO company, which is focused on reducing unproductive times through the use of time and movement study techniques. The applied methodology was of a qualitative-quantitative type due to the fact that data was collected through direct observation and interview, in addition to the processing time for each task, cycle time of the production process, number of operators, process flow and conditions. current production. On the other hand, secondary data, which included a brief history and organizational structure of the company and effective working hours. From the information obtained, several products that are made in the company were identified, so the ABC classification method was applied, where it is concluded that the product to be analyzed is the polo shirt because it is the one with the highest demand and valorization. for the company. Activity and analysis diagrams were used for each process, as well as time and movement study formats, in the measurement of the work it was obtained as a result, that the bottleneck is the manufacturing area since it is where they carry out the greatest amount operations and therefore entails a longer production time, the current standard time for the production of polo shirts was obtained from the analysis, which was 36.99 minutes. An improvement proposal was developed based on the study of times and movements where it is proposed, the standardization of operations, a new work methodology, the redistribution of machines and also, the organization of the work space to facilitate the search for materials and equipment through the 5s methodology, where the new standard time is obtained as a result, which is 32.70 minutes, which translates into an increase of 779 polo shirts per month to 881, that is, an improvement of 13% compared to the method current.